Several studies have shown that flying electric between the so-called ABC-islands in the Caribbean (i.e., Aruba, Bonaire and Curaçao) is feasible with the upcoming first generation of battery-electric aircraft. This paper presents a real-world case study that deals with the technical and operational characteristics of electric flight in that region. With that purpose, the Aruba Airport Authority (AAA) commissioned this investigation, which involved numerous local stakeholders, such as airlines, energy providers and navigation services. This study involves two commuter electric aircraft under development, aiming to investigate how they fit in the current operational scheme of three local airlines and three conventional aircraft types in terms of technology, capacity, schedule, performance, CO2 emissions and fuel costs. Conclusions indicate that a transition to batter-electric aircraft is feasible with regards to the aforementioned criteria and with the current technology and energy density of batteries.
This paper presents how the application of the STPA method might support the evaluation of fighter pilots training programs and trigger procedural and technological changes. We applied the STPA method by considering the safety constraints documented in the Standard Operating Procedures (SOPs) of a South European Air Force and regard a flight of a two F-16 aircraft formation. In this context, we derived the control actions and feedback mechanisms that are available to the leader pilot during an Aircraft Combat Maneuver (ACM) mission, and we developed the control flow diagram based on the aircraft manuals. We compared the results of each analysis step with the respective flight training program, which is based on a mixed skill and rule-based decision-making, and we examined the role of the feedback mechanisms during multiple safety constraints violations. The analysis showed that: the flight training program under study does not structurally include cases of infringement of multiple safety constraints; the maintenance of some safety constraints are not supported by alerts, or rely on only one human sense; the existing procedures do not refer to the prioritization of pilot actions in cases of violation of multiple safety constraints; operation manuals do not address the cases of possible human performance deterioration when simultaneous information from feedback mechanisms is received. The results demonstrated the benefits of the STPA method, the application of which uncovered various inadequacies in the flight training program studied, some of them related to the F-16 cockpit ergonomics. The analysis lead to recommendations in regard to the amendment of the corresponding fighter pilots training program, and the conduction of further research regarding the aircraft – pilot interaction when multiple safety constraints are violated. The approach presented in this paper can be also followed for the (re)evaluation of flight training schemes in military, civil and general aviation, as well by any human-machine interface intensive domain.
This work focuses on humidity effects of turbofan engines, in order to identify the magnitude of the error in operational conditions and the implications on maintenance decision support. More specifically, this paper employs a set of different methods, including semi-empirical corrections used in engine test beds, performance simulation models and analysis of historical data, in order to investigate the effects of humidity. We show that varying humidity can have a noticeable influence on the performance of the engine. These discrepancies cannot be currently quantified by health monitoring systems. Simulation and test bed correlations indicate a decrease of EGT of 0.35% per 1wt% of absolute humidity, which varies worldwide between 0 and 3wt%. Consequently, deviations in EGTM can be up to 1%, a figure which can be up to 12K for a modern civil turbofan. In practice, variations in ambient humidity have the potential to conceal possible deterioration in engine components. Following, the flight historical data were corresponded to historical humidity data. The two methods were identified to provide comparable results, indicating a higher EGTM for increasing ambient humidity. Overall, it was concluded that EGTM corrections for ambient humidity is an area of significant interest, especially for newer engine types where accurate diagnostics are of increasing importance.